on the second photo, the right side is underneath a standoff. try putting it above, or put the left one under
on the second photo, the right side is underneath a standoff. try putting it above, or put the left one under
I am on his team and we took off the chain on the chassis and the motors were going really slow. We don’t know what the problem is.
Problem solved.
what was the problem and the solution @Nathan?
I’ve had motors moving slowly and even stop working. In the cases which I have experienced it was due to the axle moving out of the hole, but I would like to hear your problem so if I have that same problem I can add that to my list of things to do when troubleshooting.
@meepmeepme I am on the same team as Nathan.
Well, when we programmed the robot the motor color is red torque motor and he did not put that in the program as a red torque motor.
@Ozzy LaCelle and what problem did that cause? Just low performance? I haven’t set motor gearing software side yet.
@meepmeepme It caused the motor to spin a lot slower than it would when it was programmed as the motor gears that it was supposed to.