Using VEXnet 2.0 Keys, our piston code functions abnormally. Our Cortex and Joystick are on the latest 4.1.0 firmware aswell as our keys on 1.36.
With the old 1.0 keys, the pistons toggle normally using our code, however on VEXnet 2.0 keys, the buttons read as being pressed and released multiple times. I am using RobotC 4.0. Was there a change in how the cortex and joystick communicate using 2.0 keys causing my code to malfunction?